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Due to severe compression
loss, the first task in the restoration of this tractor was an engine
rebuild. We began by removing the engine and performing a complete disassembly
and inspection. After opening the engine, we checked the crankshaft and
found it to be in excellent shape; we checked the cylinder bores and found
them to be well within specified tolerances; we cleaned the engine; we
ground the valves; we then installed standard rings and bearings after
honing the cylinders; we had the head cleaned, trued, and magnafluxed;
and we reassembled the engine using all new seals and gaskets.
After completing the engine work, we had the clutch and pressure plate
rebuilt and replaced the throw-out bearing as well. We then removed the
torque tube and installed a new transmission shaft seal and gasket. Then
we reinstalled the engine and torque tube. The next step was to disassemble
the steering system, clean the steering box thoroughly, replace the input
and output shaft seals, adjust the steering, and reassemble the steering
system and replace the lubricant. We reassembled the front end of the
tractor, swapped out the radiator for a newer radiator provided by the
owner, cleaned two inches of sludge from the bottom of the radiator tank,
and resealed the radiator during reassembly.
The next stage of the restoration included working with the rear end and
final drives. We flushed, cleaned, and inspected the interior of the transmission
and rear end. Here, we discovered what seemed to be lard, which required
extensive labor to remove and sand away rust that had built up due to
the salt in the lard. This is typically added to transmissions and rear
ends to temporarily seal leaking seals. The rear axle seals were leaking
profusely, so we replaced them. The leaking lubricants in the rear end
had caused a build up of oil/grease and subsequent collected dirt to interfere
with the operation of the brakes. We cleaned the brake bands and sanded
the brake drums. After completing these tasks, we reassembled the rear
end and moved to the final drives.
The final drive gaskets were also leaking, so we removed the final drive
pans, scraped them clean both inside and out, inspected the final drive
gears, replaced the gaskets, and refilled these pans after reassembly.
We then removed the PTO shaft, inspected the bearing, installed a new
seal, and reassembled the PTO assembly using new gaskets.
After filling all major systems with new fluids, we then temporarily wired
the tractor for a test run. We ran the tractor for approximately two hours
and inspected all work completed heretofore to ensure that no leaks appeared.
Once we ascertained that the tractor was in good working order, we began
preparing for sand blasting. This entailed additional disassembly and
covering all open access holes, shielding all gaskets and seals from the
effects of sandblasting, and removing all wheel assemblies.
After sandblasting the tractor and all of its components, including the
mower and lift components, as well as the rims, we removed all residual
sand, wiped the entire tractor and all components with paint thinner,
and began bodywork. The hood/gas tank and fenders all required major bodywork
to remove rust pits and repair dents and dings. Approximately twelve extremely
thin layers of body filler were applied on the hood and sanded according
to manufacturer recommendations. The fenders required a thin layer of
body filler over all surfaces to bring rust pits up to the height of the
surrounding metal.
Preparing the tractor for primer required additional sanding and surface
preparation with paint thinner to ensure proper paint adhesion and a smooth
finish. Pits in areas of cast iron were not filled with body filler due
to the fact that these imperfections were from the factory. However, the
front steering sector cast plug was resealed with a petroleum-compatible
epoxy and sanded relatively smoothly.
We then applied a layer of red oxide primer with hardener to every tractor
surface and all additional components (except for the exhaust manifold
and pipe). After this layer cured, we applied one layer of International
Harvester Red with hardener to all surfaces except for those areas indicated
earlier and components that would receive other paints. Once this first
layer of paint was tacky, we applied a second layer. Other components
received two layers of their respective paints as well; this includes
the exhaust assembly, electrical system components, the mower, and outer
rim flanges. The floor pan was prepared for an anti-skid coating and two
layers of this were applied. A UV-resistant coating was also applied over
the anti-skid to prevent deterioration. Once all paint cured properly,
we reassembled the tractor and all components. After reassembly, the steering
wheel and gearshift knob were repaired with epoxy, sanded, and hand-painted
with a plastic-specific paint. We then applied all decals, and re-installed
the wiring harness, a new battery, new rear tires, a new generator belt,
new oil filter, new ammeter (provided by owner), new dash-mounted oil
pressure gauge, and new muffler (also provided by the owner).
During reassembly, a piece of the governor control rod that had been improperly
welded, prior to the restoration by a former owner, broke off. We replaced
this component, and, in the process of doing so, the governor and magneto
came out of sync. Subsequent troubleshooting and inspection required that
we replace the spark plugs and wires, install a new coil, and new distributor
cap. These components were found to be worn and in need of replacement.
We then started the tractor and the owner picked up the tractor.
Due to obscure changes in the rear main seal (the manufacturer discovered
a fault in the seal plate and changed the type of seal required for certain
seal plates), an oil leak developed after the tractor went through several
heating/cooling cycles. We performed additional research regarding the
rear main seal and plate. After discovering the post-production changes,
we installed a new, updated seal and reassembled the tractor. We then
tested the tractor thoroughly, running the engine and testing every system
repeatedly over the course of four days.
This restoration
was commissioned by the owner, a gentleman in North Carolina.
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